|
Sign in using an external account
|
|
|||||||||
| Notices |
![]() |
|
|
Thread Tools | Search this Thread | Display Modes |
|
|
#1 |
|
Junior Member
Garage is empty, add now
Join Date: May 2004
Posts: 1,122
|
trying to figure out if my n75 is causing my low boost problems. i pressure tested the car about a month ago and everything looked good. Im only making 16psi at redline. Sometimes i spike to 24 and taper down, and sometimes i spike to 20 and taper down. Im not throwing any codes and i have new 710Ns. I logged block 114 but im not sure how to interpret n75 duty cycles. TIA Fats times are also down to 4.0-4.1 when they used to be 3.5-3.6
__________________
![]() ![]() ASP DPs w/ AWE Twin1 Exhaust Southbend Stg5 Feramic clutch AWE LWFW H&R Bilstein Samco EVO intake Neuspeed SS APR Snub RS4 MM RS4 Front Bumper and grille SSR Comps, Pilot cup sport:Track OZ SL Custom Paint, Nitto 555:Street 3.29 FATS on 100oct |
|
|
|
|
|
#2 |
|
Member
Garage is empty, add now
Join Date: Mar 2004
Posts: 2,951
|
__________________
"No, a flux capacitor is not compatible with a ham sandwich." |
|
|
|
|
|
#3 |
|
AudiWorld Super User
Garage is empty, add now
Join Date: Dec 2002
Posts: 2,719
|
__________________
2000 Audi S4 STG 3 FATS = 3.66 w/ 91 oct AIM: EdyJun ![]() 11 September 2001 In their honor. In their memory. <font color="red">---------------------------------------------------------- <u><big> ![]() <a href="http://homepage.mac.com/edyjun1/S4/index.htm">EdyJun's S4 Directory (FAQ, DIY, Info, Tips and Help) </a> </big> </u>---------------------------------------------------------- </font> |
|
|
|
|
|
#4 |
|
Junior Member
Garage is empty, add now
Join Date: May 2004
Posts: 1,122
|
__________________
![]() ![]() ASP DPs w/ AWE Twin1 Exhaust Southbend Stg5 Feramic clutch AWE LWFW H&R Bilstein Samco EVO intake Neuspeed SS APR Snub RS4 MM RS4 Front Bumper and grille SSR Comps, Pilot cup sport:Track OZ SL Custom Paint, Nitto 555:Street 3.29 FATS on 100oct |
|
|
|
|
|
#5 |
|
AudiWorld Super User
Garage is empty, add now
Join Date: Apr 2000
Posts: 3,686
|
I'd expect the N75 duty cycle to increase as the ECU tries to increase the actual boost toward requested.
Have you tried disconnecting the ECU and then logging that stuff after it has been reset? Might be interesting to see what happens when the system has a fresh look at the conditions.
__________________
www.MyAudiS4.com/vast-sucks (Updated: 20 Jan 2012) Stock -> APR Stg1/2 -> GIAC Stg2 -> APR K04 Stg3 -> EPL TiAL 605 -> V̶A̶S̶T̶ EPL/Frankenturbo F4H |
|
|
|
![]() |
| Tags |
| bad, disconnecting, mbc, n75 |
«
Previous Thread
|
Next Thread
»
| Thread Tools | Search this Thread |
| Display Modes | |
|
|
Powered by vBulletin® Version 3.7.5
Copyright ©2000 - 2012, Jelsoft Enterprises Ltd.
Copyright ©2000 - 2012, Jelsoft Enterprises Ltd.
Copyright 2009 AudiWorld.com Audi Enthusiast Community











Linear Mode
