nDBW K04 low on boost
#1
nDBW K04 low on boost
'97 TQM, K04, GIAC, 5 bar FPR, stock injectors/SIMC/plugs, Borla cat-back
I've had a longstanding misfire issue under load that seemed to get worse last week to the point I could only build 1-2 lbs of boost. I built the home-brew pressure tester shown in tons of threads and found 2 significantleaks,and repaired both. After that could still only get 5lbs of boost. Replaced plugs (stock) and no major improvement. I ran out of time to mess with it myself, and took it to my go-to guy for repairs. They replaced the #4 coil pack (probably cause of longstanding misfire) and repleced my N75J valve with stock N75 and replaced my ancient leaking TurboXS diverter valve with stock. The car runs great now, no CEL, no misfires, but ouly builds/holds about 14lbs of boost (used to be anywhere from 17-21).
The only other known issue with the car is a seeping valve cover gasket (oil buildup around top of plugs noticed when swapping).
Any ideas what could be the reason for the reduced boost?
I've had a longstanding misfire issue under load that seemed to get worse last week to the point I could only build 1-2 lbs of boost. I built the home-brew pressure tester shown in tons of threads and found 2 significantleaks,and repaired both. After that could still only get 5lbs of boost. Replaced plugs (stock) and no major improvement. I ran out of time to mess with it myself, and took it to my go-to guy for repairs. They replaced the #4 coil pack (probably cause of longstanding misfire) and repleced my N75J valve with stock N75 and replaced my ancient leaking TurboXS diverter valve with stock. The car runs great now, no CEL, no misfires, but ouly builds/holds about 14lbs of boost (used to be anywhere from 17-21).
The only other known issue with the car is a seeping valve cover gasket (oil buildup around top of plugs noticed when swapping).
Any ideas what could be the reason for the reduced boost?
#2
Keeper of the Cash
You didn't mention anything about your DV. Also, after 12 years I bet your fuel injector
o-rings are quite tired and should be replaced.
You say stock plugs, so are they Bosch plugs then? When were they last replaced?
Between those two and your leaky VCG, I'd say that's where your boost is going.
Just my 2ยข.
You say stock plugs, so are they Bosch plugs then? When were they last replaced?
Between those two and your leaky VCG, I'd say that's where your boost is going.
Just my 2ยข.
#4
Re: "and replaced my ancient leaking TurboXS diverter valve"
Probably, but I can do that tonight as well. My previous experience has been that if the wastegate line is messed-up, you get erratic boost and surging. This is rock-solid at about 14lbs.
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